Upload
deidre-whitfield
View
22
Download
0
Embed Size (px)
Citation preview
3M Automotive Aftermarket Division3M Automotive Aftermarket Division Bringing back that new feeling faster, easier, safer.
Line 23 Problem
Solving Lean Kaizen Project
June 30th 2016
Deidre S. Whitfield
Line 23
Alloyd Automatic Heat Seal Machine
AADAutomotive Aftermarket Division
Line 23 Products:
20058
801
930 / 930C
901 / 901C
928 806 / 806C
907 / 907C / 907ES
280 / 280ES
913 / 913C
Problem Statement:
1. Completed Lean Training week ready to research and analyze all issues on the line
2. Improve and implement all new changes in order to reduce down-time by 75% and reduce labor revenue at a cost of $90,000 per year
3. Engaged the help and cooperation from Quality, Engineering, Supervisors, Supply Chain, Management, and Operators
LINE 23 DOWN-TIME
Method
Material Machine
Fishbone Diagram:
Print / Apply Labeler
2x4 / 6x4 Size ELC Labels
Small / Big Product Tubes
5 Different types of Boxes
Altering Label to meet current Packaging Specifications
Hand-Label / Date-Code / Apply Diamond (Product Specific)
Line Shuts Down for Labeling
Environment
PeopleMeasurement
Line runs only some shifts
Operators
Engineers
ELC Programmer
Extra Labor Hours in IMES
Additional Labor (Crew) Depending on Product
Line is used as a GO TO Line
2x2 Limited Quantity Diamond
Supervisors / Management
Corporate
Supply Chain
280 / 280ES ISSUES
Found huge down-time issues on one particular product Operators/Laborers shut down the line to re-apply Date-Code Operators/Laborers manually placed custom label(s) to outer
box during shut down
280 / 280ES Improvement Solutions
Get consensus to have Date-Code on inner product and outer boxes only
Modify outer box to have pre-printed DOT Symbols needed Updated all packaging standards to inform all operators and
laborers of new changes, and implementations
Box Optimization
Issues: 5 boxes
1 size tube in 3 different box sizes
Longer changeover time due to multiple RM changes
Box Optimization
Solutions:• Consolidate to 4 boxes
Streamline all big tubes to high volume box
Have all small tubes in same size box (Not 3 Different Boxes)
• Change label size to fix new box size
Box Labeling Project:Issue: • Operators/Laborers shut down line to hand
label some productsWhy?
• ELC labels not configured to:Print one at a timePrint on right size labelPrint orient upside down
Solution: • Create matrix of products and specs needed
• Contact Corporate ELC Support to fix issues
• Work with Lean Leads to verify implementation
Label Machine Programmed for PNO907
Graph Improvement:
• Tracked down-time relating to 280 / 280ES, Box and ELC Label issues for a total of 8 weeks
• During this tracking period, a totaled cost of $20,000 was due to these surrounding issues
Expected results after implementation:
• Reduce down-time by 75%
• Projected labor savings of $90,000 per year.
Final Summary280 / 280ES Improvement
Project:James MartinekBrenda Narcisse
Matt GaynerDeidre Whitfield
John Howell
Box Labeling Project:
James MartinekDeidre Whitfield
Matt GaynerRehan Khan
Courtlind Miller
Box Optimization Project:James MartinekPatricia Chee
Deidre WhitfieldCharles Hughes
Cross functional team across Operators, Supervisors, Engineers, Quality, and Supply Chain 1 Lean Kiazen event with 4 follow-up meetings with sub teams
Learned how to get buy-in from a variety of groups Tapped into Corporate’s resources for packaging and ELC changes
Operators are energized that we are eliminating extra work that appeared to have no benefit
3M Automotive Aftermarket Division
Questions?